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Docket ID: [Docket No. FAA-2008-0649; Directorate Identifier 2008-CE-038-AD]
RIN ID: RIN 2120-AA64
SUBJECT CATEGORY: Airworthiness Directives; DG Flugzeugbau GmbH Model DG-500MB Powered Sailplanes
DOCUMENT SUMMARY: We propose to adopt a new airworthiness directive (AD) for the products listed above. This proposed AD results from mandatory continuing airworthiness information (MCAI) originated by an aviation authority of another country to identify and correct an unsafe condition on an aviation product. The MCAI describes the unsafe condition as:
A DG500MB experienced, after the engine shutdown, an uncommanded retraction of its powerplant.
Investigations revealed that some bolts of the extension retraction mechanism had fractured because of fatigue stress due to increasing pushpull loads acting on incorrectly tightened screws.
This condition, if not corrected, could lead to damage of the propeller and the fuselage, thereby reducing the structural integrity of the sailplane.
The proposed AD would require actions that are intended to address the unsafe condition described in the MCAI.
SUMMARY: DG Flugzeugbau GmbH Model DG-500MB Powered Sailplanes,
We invite you to send any written relevant data, views, or arguments about this proposed AD. Send your comments to an address listed under the ADDRESSES section. Include ``Docket No. FAA20080649; Directorate Identifier 2008CE038AD'' at the beginning of your comments. We specifically invite comments on the overall regulatory, economic, environmental, and energy aspects of this proposed AD. We will consider all comments received by the closing date and may amend this proposed AD because of those comments.
We will post all comments we receive, without change, to http:// www.regulations.gov, including any personal information you provide. We will also post a report summarizing each substantive verbal contact we receive about this proposed AD.
The European Aviation Safety Agency (EASA), which is the Technical Agent for the Member States of the European Community, has issued EASA AD No. 20080095, dated May 16, 2008 (referred to after this as ``the MCAI''), to correct an unsafe condition for the specified products. The MCAI states:
A DG500MB experienced, after the engine shutdown, an uncommanded retraction of its powerplant.
Investigations revealed that some bolts of the extension retraction mechanism had fractured because of fatigue stress due to increasing pushpull loads acting on incorrectly tightened screws.
This condition, if not corrected, could lead to damage of the propeller and the fuselage, thereby reducing the structural integrity of the sailplane.
To address this unsafe condition, this Airworthiness Directive mandates the replacement of eight bolts, the four connecting the fork 5M203 to the 5M204 adapter and those connecting the adapter 5M204 to the spindle drive, by new ones of higher strength and a rework of the coupling of the 5M203 fork to the 5M204 adapter as well as the coupling of the 5M204 adapter to the spindle drive, by glueing the parts together, in addition to the preexisting bolts.
You may obtain further information by examining the MCAI in the AD docket.
DG Flugzeugbau GmbH has issued Technical Note No. 843/27, dated April 14, 2008. The actions described in this service information are intended to correct the unsafe condition identified in the MCAI. FAA's Determination and Requirements of the Proposed AD
This product has been approved by the aviation authority of another
country, and is approved for operation in the United States. Pursuant
to our bilateral agreement with this State of Design Authority, they
have notified us of the unsafe condition described in the MCAI and
service information referenced above. We are proposing this AD because
we evaluated all information and determined the unsafe condition exists
and is likely to exist or develop on other products of the same type design.
Differences Between This Proposed AD and the MCAI or Service Information
We have reviewed the MCAI and related service information and, in general, agree with their substance. But we might have found it necessary to use different words from those in the MCAI to ensure the AD is clear for U.S. operators and is enforceable. In making these changes, we do not intend to differ substantively from the information provided in the MCAI and related service information.
We might also have proposed different actions in this AD from those in the MCAI in order to follow FAA policies. Any such differences are highlighted in a NOTE within the proposed AD.
We estimate that this proposed AD would affect 4 products of U.S. registry. We also estimate that it would take about 3 workhours per product to comply with the basic requirements of this proposed AD. The average labor rate is $80 per workhour. Required parts would cost about $63 per product.
Based on these figures, we estimate the cost of the proposed AD on U.S. operators to be $1,212, or $303 per product.
Title 49 of the United States Code specifies the FAA's authority to issue rules on aviation safety. Subtitle I, section 106, describes the authority of the FAA Administrator. ``Subtitle VII: Aviation Programs,'' describes in more detail the scope of the Agency's authority.
We are issuing this rulemaking under the authority described in ``Subtitle VII, Part A, Subpart III, Section 44701: General requirements.'' Under that section, Congress charges the FAA with promoting safe flight of civil aircraft in air commerce by prescribing regulations for practices, methods, and procedures the Administrator finds necessary for safety in air commerce. This regulation is within the scope of that authority because it addresses an unsafe condition that is likely to exist or develop on products identified in this rulemaking action.
We determined that this proposed AD would not have federalism implications under Executive Order 13132. This proposed AD would not have a substantial direct effect on the States, on the relationship between the national Government and the States, or on the distribution of power and responsibilities among the various levels of government.
For the reasons discussed above, I certify this proposed regulation:
1. Is not a ``significant regulatory action'' under Executive Order 12866;
2. Is not a ``significant rule'' under the DOT Regulatory Policies and Procedures (44 FR 11034, February 26, 1979); and
3. Will not have a significant economic impact, positive or negative, on a substantial number of small entities under the criteria of the Regulatory Flexibility Act.
We prepared a regulatory evaluation of the estimated costs to comply with this proposed AD and placed it in the AD docket. List of Subjects in 14 CFR Part 39
Air transportation, Aircraft, Aviation safety, Safety. The Proposed Amendment
Accordingly, under the authority delegated to me by the Administrator, the FAA proposes to amend 14 CFR part 39 as follows: [[Page 33745]]
1. The authority citation for part 39 continues to read as follows:
Authority: 49 U.S.C. 106(g), 40113, 44701.
2. The FAA amends Sec. 39.13 by adding the following new AD: DG Flugzeugbau GmbH: Docket No. FAA20080649; Directorate
Identifier 2008CE038AD.
Comments Due Date
(a) We must receive comments by July 14, 2008.
Affected ADs
(b) None.
Applicability
(c) This AD applies to DG500MB powered sailplanes, all serial numbers, certificated in any category.
Subject
(d) Air Transport Association of America (ATA) Code 71: Power Plant.
Reason
(e) The mandatory continuing airworthiness information (MCAI) states:
A DG500MB experienced, after the engine shutdown, an uncommanded retraction of its powerplant.
Investigations revealed that some bolts of the extension retraction mechanism had fractured because of fatigue stress due to increasing pushpull loads acting on incorrectly tightened screws.
This condition, if not corrected, could lead to damage of the propeller and the fuselage, thereby reducing the structural integrity of the sailplane.
To address this unsafe condition, this Airworthiness Directive
mandates the replacement of eight bolts, the four connecting the
fork 5M203 to the 5M204 adapter and those connecting the adapter
5M204 to the spindle drive, by new ones of higher strength and, a
rework of the coupling of the 5M203 fork to the 5M204 adapter as
well as the coupling of the 5M204 adapter to the spindle drive, by
glueing the parts together, in addition to the preexisting bolts. Actions and Compliance
(f) Unless already done, within the next 30 days after the
effective date of this AD, modify the spindle drive assembly in
accordance with DG Flugzeugbau GmbH Technical Note No. 843/27, dated April 14, 2008.
Note: This AD differs from the MCAI and/or service information as follows: No differences.
Other FAA AD Provisions
(g) The following provisions also apply to this AD:
(1) Alternative Methods of Compliance (AMOCs): The Manager,
Standards Office, FAA, has the authority to approve AMOCs for this
AD, if requested using the procedures found in 14 CFR 39.19. Send
information to ATTN: Greg Davison, Aerospace Engineer, FAA, Small
Airplane Directorate, 901 Locust, Room 301, Kansas City, Missouri
64106; telephone: (816) 3294130; fax: (816) 3294090. Before using
any approved AMOC on any powered sailplane to which the AMOC
applies, notify your appropriate principal inspector (PI) in the FAA
Flight Standards District Office (FSDO), or lacking a PI, your local FSDO.
(2) Airworthy Product: For any requirement in this AD to obtain
corrective actions from a manufacturer or other source, use these
actions if they are FAAapproved. Corrective actions are considered
FAAapproved if they are approved by the State of Design Authority
(or their delegated agent). You are required to assure the product is airworthy before it is returned to service.
(3) Reporting Requirements: For any reporting requirement in
this AD, under the provisions of the Paperwork Reduction Act (44
U.S.C. 3501 et seq.), the Office of Management and Budget (OMB) has
approved the information collection requirements and has assigned OMB Control Number 21200056.
Related Information
(h) Refer to MCAI European Aviation Safety Agency (EASA) AD No.
20080095, dated May 16, 2008; and DG Flugzeugbau GmbH Technical
Note No. 843/27, dated April 14, 2008, for related information.
Issued in Kansas City, Missouri, on June 6, 2008. David R. Showers,
Acting Manager, Small Airplane Directorate, Aircraft Certification Service.
[FR Doc. E813324 Filed 61208; 8:45 am]
BILLING CODE 491013P
FOR FURTHER INFORMATION CONTACT Gregory Davison, Aerospace Engineer, FAA, Small Airplane Directorate, 901 Locust, Room 301, Kansas City, Missouri 64106; telephone: (816) 3294130; fax: (816) 3294090.
14 CFR Part 39 40 CFR Part 52 14 CFR Part 71 33 CFR Part 165 47 CFR Part 73 26 CFR Part 1 50 CFR Part 679 40 CFR Part 180 50 CFR Part 17 33 CFR Part 117 44 CFR Part 67 50 CFR Part 648 14 CFR Part 97 40 CFR Part 63 6 CFR Part 5 33 CFR Part 100 50 CFR Part 622 50 CFR Part 660 26 CFR Part 301 44 CFR Part 65 39 CFR Part 111 40 CFR Part 271 40 CFR Part 300 47 CFR Part 64 40 CFR Parts 52 and 81 50 CFR Part 665 39 CFR Part 3020 50 CFR Part 229 44 CFR Part 64 49 CFR Part 571